Performance Enhancement, Power Reduction, and other Flight Concerns - Testing of the CO <sub>2</sub> Removal Assembly for ISS

1999-01-2111

07/12/1999

Event
International Conference On Environmental Systems
Authors Abstract
Content
This paper describes testing of four-bed molecular sieve (4BMS) development hardware in support of future operations of the International Space Station (ISS) Carbon Dioxide Removal Assembly (CDRA). During 1998, testing of a MSFC 4BMS included operations with the 4BMS inlet air drawn directly from the cabin atmosphere instead of the baseline air source downstream of a Condensing Heat Exchanger (CHX), operating with high carbon dioxide (CO2) loading, and long duration operation in a power save mode. Additionally, testing with increased coolant water temperature was performed to determine effects on the systems CO2 removal performance.
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DOI
https://doi.org/10.4271/1999-01-2111
Pages
10
Citation
Knox, J., and Howard, D., "Performance Enhancement, Power Reduction, and other Flight Concerns - Testing of the CO 2 Removal Assembly for ISS," SAE Technical Paper 1999-01-2111, 1999, https://doi.org/10.4271/1999-01-2111.
Additional Details
Publisher
Published
Jul 12, 1999
Product Code
1999-01-2111
Content Type
Technical Paper
Language
English