Development and Flight Testing a Simplified Fixed Shaft Turboprop Flight Control System

660218

02/01/1966

Event
2nd Annual Business Aircraft Conference
Authors Abstract
Content
Adaptation of fixed shaft turboprop engines to business and utility aircraft requires drastic simplification of the control system as compared to transport turboprops. The AiResearch TPE331 engine incorporates a variable low pitch stop controlled thru mechanical linkage to achieve both simplified control and also reverse thrust. Control of the system utilizes a cam cut to match airplane-engine-propeller flight characteristics. Flight testing in aircraft varying from a converted B-26 test bed to slow STOL aircraft was used to verify calculations and develop control system, negative torque system and general engine development.
Meta TagsDetails
DOI
https://doi.org/10.4271/660218
Pages
8
Citation
Johnson, V., Baker, J., and Massey, J., "Development and Flight Testing a Simplified Fixed Shaft Turboprop Flight Control System," SAE Technical Paper 660218, 1966, https://doi.org/10.4271/660218.
Additional Details
Publisher
Published
Feb 1, 1966
Product Code
660218
Content Type
Technical Paper
Language
English